Friday, February 25, 2022

Hardinge CHNC Lathe Project Catch-up Update - Part 2

Hello Everyone,

As I mentioned in the last updates, there was not a lot going on in the Prowler world between late 2020 and early 2021.  Also, I was not working the "day job" because of CoVid.  So, I took advantage of the time to get some machine fixing done. 

CAUTION ! - This blog update does not contain any Prowler related material.  If you don't care to see me talk a lot about repairing old machines, you might want to skip ahead to the next blog update.

The (Seemingly Never Ending) Hardinge CNC Lathe Project
This machine has been sitting in the shop bay where I normally work on projects for so long, that it starting to become a permanent fixture.  I really need to get this machine out of the shop! (I need the space!)  So, I put my head down and charged forward on several "hit list" items on this never ending repair/remodel/restore project. 

Tool Turret - This CNC lathe originally had an 8 position tool turret that could automatically be lifted up, rotated to a new tool, and then locked back down into position.  There were an amazing amount of special parts that worked in concert to accomplish this seemingly simple function.  When the F8025T control was retrofitted to this machine, the old control was removed and this rendered the automatic tool selection turret unusable. 

The retrofit installer's solution was to bolt a bar of steel to the turret and turn it into a gang bar style tool setup.  That did work, and there are many gang bar style tool machines out there.  However, the range of motion of this machine in the X axis is a little limited (short).  So, it cuts down on the number of tools you can mount onto it.....depending on the size of your stock, etc.  The other problem was that air was no longer ported to the side of the piston to hold the turret down firmly, so it allowed for some tool movement - affecting accuracy.

I really didn't like this idea of a gang tool bar and I wanted to figure out a way to make the tool turret usable again.  However, to get this to work again automatically with the F8052T control was going to be a real challenge.  But, even if it wasn't automatic, if I could just get the turret to pop up and rotate by hand, that would be a huge improvement.  After some more tear-down of the cross-slide and tracing some air channels in there I decided it might be possible.  Using a small number of the original parts, and adding an "air switch" the turret could maybe be used again to select new tools in a manually selectable fashion.

In it's original form, what made the turret lift up and lock down was simply air pressure ported to a piston that was integral and attached to the tool turret.  If I could figure out a way to get air routed properly to that piston, I could make it move again.  The hole in the cross slide in the picture below is essentially the "cylinder" of a pneumatic actuator:
This (below) is the air piston that is integral to the turret.  The tool turret plate is attached with the nut on the right side.  The black stripe around the edge of the piston is the large O ring that seals the piston inside the cylinder:
Here is the piston mounted into the cylinder.  The tapered dogs on the left and the right are what align the turret plate to the lathe and help hold it in position when air pressure pushes the piston down.  The turret plate rotates using the bearing on the inside diameter you see here:
Put it all together and you get this:
Now, to move the turret up or down, air pressure has to be applied to either the bottom and vented off the top, or vice-versa.  That required finding the original ports that would take the air pressure to the top side and bottom side of the air piston.  Once i found those, I simply had to plumb them to this special "air switch" that I found online:
This switch has 3 positions: 1- a position that just vents all the lines;  2. - Port A pressurized and port B vented;  and, 3. - Port B pressurized and port A vented.   Here is the air switch mounted into the machine (before paint):
I added pressurized air to the machine and got this:
YES!  It works!!  With this setup, the machine can now be programmed to work with one tool, then use a pause routine with a message for the operator to select the new tool, then press the cycle/start button to continue operation.  Sweet!

Spindle Encoder Cover - A spindle motor encoder is a device which sends feedback information from the spindle motor back to the machine control (computer).  It is a rotatory device that is mechanically linked to the spindle motor and always turns whenever the spindle motor turns.  It essentially sends a stream of electrical pulses to the control computer and the computer can count these pulses and accurately determine the spindle speed, direction of rotation and angular position.  Here is the spindle encoder on this machine:
As was the case with so much of this machine, when the new control was installed, many of the original supporting components were left in place and just disabled.  The spindle encoder system was no different.  In fact, as I started to troubleshoot this system, I found the spindle encoder cable cut in half and the ends of the cables simply stuffed into cable way tubes!  The other thing I determined while troubleshooting this system was that the original encoded was not working correctly (probably why the cable was cut). 

The encoder you see in the picture above was an older, used unit I found online to replace the original.  Once installed and working, it needed a cover.  The original cover could not be found, so I decided to fabricate a new one.  The first step was to make a plate to fit the mounting surface on the machine.  Using a picture of the pad and scaling it in the CAD software, I was able to use the CNC mill to cut this plate out:
Then, I found a piece of aluminum tubing the correct size and cut a piece to the right length.  The one mounting hole in the flange was going to get partially covered by the piece of round tubing, so I used the mill to cut a partial hole (groove) in the right place:
So far, so good:
Add a cover and here is the result tack welded together:
I will get this welded up soon and finally get it installed on the machine.

Collet Closer - The next system on this lathe that needed attention was the collet closer system.  This machine was designed to use 5C collets and the are tightened by an air diaphragm system pictured below. 
When I bought the machine, the parts V & X shown in the picture below were missing.  Fabricating these parts was going to be a pretty big job. 
Fortunately, the buddy I bought the machine from was converting one of his other Hardinge lathes over to a newer style collet system and could give me these parts off of his machine.  So that part of the system was taken care of.  Here they are installed on my machine:
With that done, I turned my focus another part of this collet closer system.  The air glands and piston.  While researching this part of the lathe, I learned that this model of collet closer uses a lot of air - even when they are new and working correctly.  The reason is that there are not any seals in the system between the rotating and stationary parts of the closer - only tight tolerance air glands that are located in part where the air lines attach in the picture above (on the left side of part Q).  I decided to go through the entire part Q and replace all the seals, just to make sure it won't give any problems later.  So, here is a picture of the closer piston taken apart:
I actually posted a YouTube video of this work, in case it might help someone else refurbish their unit some day.  If you are interested, you can see it here:  Vari-Grip Collet Closer

With the unit re-sealed, I installed it back onto the machine and hooked up the air lines:
Now, I had to resurrect the part of this system that applied the air to the closer to get it to open and close.  In it's original form, this collet closer was controlled by a switch on the old, 1970's vintage controller console - which is long gone.  What that switch did, was control two solid state relays that I had earlier relocated to the new electronics cabinet.  You can see the bank of relays in this picture:
So, all I had to do was to source a new switch and wire it to control those same 2 relays.  Then, I would have to mount the switch in a convenient place for the operator to control.  I ended up finding a rotary switch and then fabricated a switch box with a switch guard to mount to the front of the machine.  Here are the parts that I fabricated and the switch:
The parts assembled and before paint:
And, here is a picture of the switch box mounted to the front of the machine:
Just below this new switch is the solenoid compartment.  Each of the two solenoids controlled by the new switch are in this compartment (pictured below).  This system is called "Vari-Grip" and what it means is that it can adjust how tightly the collet clamps down on the parts being machined.  The "Vari" in this systems simply comes from an air pressure regulator that controls the amount of air pressure sent to the "Grip" part of the system.  You can see this pressure regulator in the upper left of the picture below.
The solid state relays control two solenoids that are located the the far bottom left of the pic above.  The two larger black air hoses in the far left side of the picture are the air lines that pass through the machine walls and end up coming out behind the headstock and go to the collet closer shown in a picture (several) above.  This was my first experience dealing with a collet closer system and I learned a great deal about it.  I'm also happy to have it rebuilt and done!

Coolant Tank and Pump - Well, of all the repairs to this machine so far, it was this coolant tank system that almost broke me!  In order to get the old tank out of the machine, there is a sleeve between the catch pan and the top of the tank that must be pulled upward.  In order to pull that sleeve up, I had to remove a plug that had been welded into the bottom of the catch pan.  Removing that plug was a bear!!  I played hell trying to get that thing cut loose and pulled up, out of the way.  I heat it, beat it, ground on it, pried on it, and it wouldn't budge.  Finally, I had to weld bolts to the inside and then block up a strong back to pull it up with 3/8" nuts.  Just look at this thing:
BTW - wrestling with this thing was made worse by the fact that it was directly under the bed of the lathe.  Once I got the the plug removed from the catch pan, I was able to remove the sleeve from the hole in the top of the coolant tank can see in this pic below.  This pic is of the coolant tank after I remodeled it to about 1/3 of it's original size and welded some fittings into it.  The fitting with the hose on it is the pump pick-up.  The one below that is for a drain valve.  Here is the tank while testing my welds for leaks with water:
The same tank after some clean-up and some paint:
Here is the tank put back into the machine with the coolant level indicator that I made viewable from the back of the machine:.  There will eventually be a panel in place to cover this tank access with a window for viewing the coolant level:
Here is another view of the tank installed in the machine.  The pump is on the right side and the lower left side has a drain valve on the bottom and a tank suction for the pump just above.  You can also see the sleeve that comes down from the catch pan and seals into the hole in the top of the tank:
To get the coolant pump to work both in manual and automatic (activated by the part program) - I had to find the control wires and route them to one of the solid state relays in the servo control cabinet.  In this case, it is 5CR, the relay in the top right that is wired to the coolant pump:
With that wiring completed, I did a test of the system in this video:
The last step to the coolant tank work was to fabricate a new screen to put in the bottom of the catch pan (instead of a plug) to catch fine chips from making their way into the coolant tank.  I found a piece of pipe the correct size, welded a steel screen to the bottom and put it in place:
After getting the plug out of this system, the all was academic after that.  Glad to have this system working again.

Control Cabinet - There were several modifications that I wanted to make to how this control was mounted and located.  The first one was that I wanted to install a PC that could be used to transfer programs to/from the F8025T.  The second thing I needed to do was to move where the control was mounted to the machine, because 2 of the main cables running to the servos stuck out of the side of the control cabinet in a way that the door by the operator's station could not be closed all the way.  Then, as I got more into this part of the project, I also decided that the control needed to be mounted to a rolling cabinet that could be disconnected when the machine had to be moved, and then moved as needed.

As I worked on a lot of the parts of this machine that I've discussed earlier and in previous updates, I was keeping my eye out for an enexpensive PC and LCD monitor.  I eventually found both and set out mount them to the existing control box.  I made a bracket that fit the monitor and used that to mount it to the top of the box.  You can see that here:
I also found some sheet metal and formed up a keyboard tray that I mounted at an angle and put a small flat shelf for the mouse pad.  It turned out pretty nice and it all worked when I plugged everything in and tried it:
Once I had this finished, I started thinking about moving this machine.  With all this "stuff" attached to the control box, how do you move it?  How do you set it down, without breaking something off or having to take it all apart?  I had to find a better way.

About that time, I came across an old steel cart that was like a podium on wheels.  I looked it over and decided that if I could cut it off the right height, weld the right plates and brackets to the top, then I could mount the control on it permanently.  With this design, moving the machine would be much easier - just removed a few canon plugs, pull a few power wires and remove a couple of bolts and the whole control cabinet would be able to be rolled away from the main machine.  Then, the main machine could be lifted with a forklift and moved as needed.  I liked the idea.  After some cutting, heating and beating, I had this:
I even put in a shelf to mount the small footprint PC to inside the cabinet.  The other nice thing about this plane is that there will be storage in this rolling cabinet to put machine manuals and spare parts etc.:
When, I put it all back together again, this is how it looked:
Nice!  So, now that I could move the control around more easily, I wanted to work on positioning it so that the control cables to the servos would not interfere with the doors on the machine.  I rolled the control back about 8 inches an now the cables to the servos will pass behind the canopy on the machine.  You can see in this pic where the control cables plug into the blue connections on the control box:
The only modification needed to make the control stay in this position can be seen in this picture:
The black square tube with the flange on the right is connected to the control box, the holes in the machine base on the left is where it used to be bolted together.  All I would need to do is fabricate a plate with hole patterns in the right places and bolt it all together.  Since the weight of the control was no longer supported by this steel tube, it did not have to be very beefy or strong.  All it would do is hold the cart in place, essentially.  Here it is, also painted up in black:
Now, the control is positioned well and sits pretty much like you saw 3 pictures above.

Paint and Panels - With the bulk of the repairs done to this machine, it was time to start putting the panels back on and I wanted to put a coat of paint on the base to clean it up a little.  I did not have all the missing panels, several were removed and not on the machine when I got it.  But, I did have a little collection of panels that I'd gotten off of other machines in the past or found various places.  I was able to find enough to replace all the panels on the machine - except one.  Here's the front of the machine:
There was a panel that covered the main spindle motor originally, but it has long since been removed and lost.  I decided to leave the machine without replacing that one cover.  Here is that end:
Here is the right end of the machine and the back with all the panels in place and painted.  The panel that covers the coolant tank in the back was the last to be fabricated, painted and put on the machine:


So, as the machine currently sits, I have a little painting to do - I want to paint the uprights on each end of the machine and repaint the doors black (they are sitting on top of the machine, up-side-down in this picture):
I have to decide if I want to spend the money to put plexiglass back in the doors.  That'd be a little expensive, and I only want to do it if there is real need for it.  I have more thinking to do on that topic.

There is also a little more sheet metal work to do on the control cabinet and that needs to be painted black.  I want to add some shelves in the cabinet for the machine manuals and paperwork.  I also would like to have a space to put some of the old/spare parts from the machine.

I will report on these items in a future update.  Thanks for checking out this project.  I hope it was informative and maybe a little entertaining.

Wednesday, February 23, 2022

Hardinge CHNC Lathe Project Catch-up Update - Part 1

Hello Everyone,

Thanks for checking out the blog.  This update is going to be dedicated to the seemingly never ending Hardinge CHNC lathe project.  First off, a warning!

CAUTION ! - This update is completely dedicated to my work on this Hardinge CHNC Lathe projetct.  There is no Prowler related material in this update.  So, if you are only interested in Prowler "stuff" - you might want to skip ahead to other updates.

With that said, I will also say that some of the information in this update may have been mentioned in previous blog updates.  My intention here is to go over some of the work that I have done to this machine that I did not want put in my normal Prowler updates.  It's a lot of info, and I try to not "clutter up" the Prowler blog updates with too much non-Prowler related info.

Power Switch
One part of this project that I've not mentioned before is the power supply for the spindle system.  After I moved all of the electrical components into the smaller compartment, I wanted to be able for the operator to turn it on from the front operator's station.  So, I sourced an appropriate switch and a box and mounted them to the front of the machine.  Here is what that turned out to look like:

F8025T Control Cooling
Another important change I made was adding ventilation to the F8025T.  Heat is the enemy of every electrical component - I cannot believe that this control cabinet was not cooled in any way.  Especially, considering that the Fagor control is in a box already - then whoever did this retrofit mounted that airtight box INISDE of another airtight box (you'll see it in few pics below).  That's a formula for certain electronics failure!  So, I found some fan screens and found an appropriate place to locate it:
Marked the mounting holes:
Then, cut air flow holes:
Test fit:
And, finally put it all together:

This setup in the back cabinet door was merely a vent for the fan air to exhaust out of the cabinet through.  I created a similar vent on the bottom of the cabinet and mounted the fan on the inside above it:
This allows the fan to blow directly up onto the control and then vent out the back of the outer control box.  Here you can see the heat sink on the back of the actual control (computer) box that is mounted inside of the outer box (which holds the rest of the servo control components):
This should help this F8025T last much longer - and the door won't have to hang open on the back of the control anymore!

RS232 Serial Connection
Here is another little facet of this project that has big returns.  The connection for the serial cable that is used to hook the control to a laptop or PC was always laying inside the back door.  I wanted to have this passing through the control wall so that it could could be connected to a PC without having to have the back door open.  All that took was a drill bit, a small grommet and about an hour with a soldering iron to make it happen.  Here was the final result:
In the next update you'll see how this serial cable is used to hook the control to a PC full time so that part files can be transfer to/from the control with ease.

Z Axis Homing Switch
Something else that was a pretty important part of this refurbish project was designing a new Z axis home switch.  When the F8025T retrofit was done to this machine, they used one of the old limit switches that was original to the 1970's CHNC design.  That switch finally became unusable (years of soaking in oil and coolant) and it was mounted in a difficult area to access.  So, I wanted to move it to a more serviceable location and replace it with a new, reliable switch. 

I sourced a good limit switch.  But, there was no convenient place to locate it where a part of the cross-slide could contact the switch as needed to set the home position.  So, I picked another convenient place to mount the switch and had to fabricate a long, rigid arm that would do the contact work: 
Another view:
This Z homing setup works excellent now.  It should provide reliable homing for many years.  Seems like a simple thing, but the amount of work and time it takes to do these little things can really add up.

New X Axis Mechanical Setup
When I bought this project, the X axis servo motor and belt system was a cobbled together, hacked up mess.  The main plate was not long enough to cover all the servo motor mounting bolts holes and an add-on plate was hacked away to allow for belt clearance.  The 48 tooth cogged belt pulley was corroded and worn until the belt would skip and slip.  All the this may not be clearly evident in this pic, but you'll get the idea:
You can really see the bad condition of the big pulley here:
All that I really wanted to do with this was to find a 1-1/2" long piece of 48 tooth cogged bar so that I could machine it to fit the existing hardware, then make a new plate for mounting the servo to the X axis cross-slide and put it together.  Well, it was not going to be that easy.  I beat up the internet for days looking for a piece of 48 tooth stock - but all I could find were wholesale vendors that wanted to sell me a 10 foot bar of this stuff at a pretty hefty cost.  That wasn't going to work.

Eventually, the best and most cost effective solution I could come up with was a retail pulley that I thought I might be able to adapt to the existing set up.  So, I took the old part that you see on the left in the picture above and cleaned it up and shortened it a bit.  Then, I put it back onto the machine:
Next, I had to machine a sleeve that would fit over the part above on the inside end, and fit the new pulley on the outside end.  This is what I came up with, initially:
Then, I fitted the pulley onto the sleeve:
After that, I started on the new servo motor mounting plate.  Here it is, cut to size and shape and getting the hole cut in for the new pulley sleeve to pass through:
And, here is the test fit up:
Now, for the holes and slots to mount the servo motor:
Next, I had to make a sleeve to mount the small pulley to the servo motor shaft.  Then, putting it all together got me to this:
This was looking and working great.  But, I decided that the pulleys were sticking out too far.  I took it all back apart and shortened the necessary pieces.  Then, I put it all back together and now, it looked "right."
This was much better.  (You might notice that I also put a larger pulley on the servo motor shaft.  I did that so that the servo shaft could pass all the way through the pulley and shorten the overall length.  However, this required some re-programming of the control to account for the new gear ratio between the servo pulley and the X axis ballscrew.)  Now, all that was left to do was make a cover to protect the belts and pulleys from coolant, etc.  I'll cover that in the next update.

Spindle Electronics Cabinet Door
Here is a quick picture of the servo control cabinet after I fabricated and mounted a door to cover the components:

That's gonna do it for this part of the lathe project update.  Part 2 will be out soon and bring us up to where the project currently is as it sits in the shop.  Thanks for checking this out.  See you in Part 2, coming up next.